ASN Wikibase Occurrence # 367344
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Date: | Sunday 4 March 1990 |
Time: | 12:00 LT |
Type: | Cessna T-50 |
Owner/operator: | Private |
Registration: | N578EK |
MSN: | 2581 |
Year of manufacture: | 1942 |
Total airframe hrs: | 4304 hours |
Engine model: | JACOBS R-755-9 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Brackettville, TX -
United States of America
|
Phase: | Initial climb |
Nature: | Ferry/positioning |
Departure airport: | |
Destination airport: | Tula Rosa, TX (NONE) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE AIRCRAFT WAS DEPARTING FROM AN AIRSTRIP ON A FERRY PERMIT FOR AN INOPERABLE LANDING GEAR MECHANISM. THE PILOT REPORTED THAT THE AIRCRAFT'S RIGHT ENGINE FAILED AT APPROXIMATELY 75 TO 100 FEET AGL DURING INITIAL CLIMB. THE PROPELLER WAS NOT OF A TYPE THAT COULD BE FEATHERED. HE STATED THAT HE WAS UNABLE TO LAND ON THE REMAINING RUNWAY AND ELECTED TO CIRCLE TO LAND. DURING THE CIRCLING MANEUVER, THE PILOT FELT THAT HE WOULD BE UNABLE TO RETURN TO THE AIRSTRIP AND ATTEMPTED TO ALIGN THE AIRCRAFT FOR LANDING ON A ROAD AHEAD OF THE AIRCRAFT. DURING A STEEP RIGHT BANK FOR THIS PURPOSE THE AIRCRAFT'S RIGHT WING STRUCK A POWER LINE, CARTWHEELED, AND COLLIDED WITH THE TERRAIN. THE ON SITE INSPECTION REVEALED THAT BOTH ENGINES WERE HAVING SOME CARBURETOR HEAT APPLIED EVEN THOUGH THE CONTROL POSITIONS WERE OFF. THE RIGHT CARBURETOR INLET SCREEN WAS VERY DIRTY AND THE ACCELERATOR PUMP WAS STUCK AT THE ONE QUARTER THROTTLE OPEN POSITION. THIS WAS NOT IMPACT RELATED.
Probable Cause: AN ENGINE FAILURE CAUSED BY A MALFUNCTIONING CARBURETOR AND THE PILOT'S MISJUDGING HIS OBSTACLE CLEARANCE WHICH RESULTED IN A WIRE STRIKE WHILE MANEUVERING TO LAND. FACTORS IN THE ACCIDENT WERE THE UNCOMMANDED DEPLOYMENT OF CARBURETOR HEAT ON BOTH ENGINES, AN INOPERATIVE GEAR RETRACTION SYSTEM, AND A PROPELLER SYSTEM WHICH COULD NOT BE FEATHERED.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW90LA078 |
Status: | Investigation completed |
Duration: | 2 years and 7 months |
Download report: | Final report |
|
Sources:
NTSB FTW90LA078
Location
Revision history:
Date/time | Contributor | Updates |
22-Mar-2024 13:23 |
ASN Update Bot |
Added |
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