Accident Beechcraft 58 Baron N6659D,
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ASN Wikibase Occurrence # 367694
 
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Date:Saturday 18 November 1989
Time:13:45 LT
Type:Silhouette image of generic BE58 model; specific model in this crash may look slightly different    
Beechcraft 58 Baron
Owner/operator:Private
Registration: N6659D
MSN: TH 1005
Total airframe hrs:1337 hours
Engine model:CONTINENTAL IO-520
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Fernandina Bch, FL -   United States of America
Phase: En route
Nature:Private
Departure airport:Metter, GA (2J4)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
DURING FLT, THE PLT NOTED THAT OIL PRESSURE IN THE RGT ENG HAD DROPPED TO THE RED LINE, SO HE SHUT DOWN & FEATHERED THE ENG. HE STATED THAT AFTER ENTERING TRAFFIC TO LND, HE 'LOWERED' THE GEAR, THEN NOTED THAT THE RADAR & RADIOS BECAME INOP (AS ELECTRICAL POWER WAS LOST). THOUGH HE HEARD & FELT THE GEAR EXTEND, HE DID NOT SEE ILLUMINATION OF THE DOWNLOCK LIGHTS. THE PLT MADE A 360 DEG TURN TO GET SPACING BEHIND ANOTHER ACFT, THEN CONTD THE APCH TO LAND. DURING THE LANDING, THE GEAR COLLAPSED & THE ACFT WAS DAMAGED. AN EXAM OF THE RGT ENG REVEALED THAT THE LOW OIL PRESSURE WAS DUE TO A PIECE OF CARBON UNDER THE OIL PRESSURE RELIEF VALVE SEAT. BOTH ALTERNATORS TESTED SATISFACTORILY; HOWEVER, BOTH VOLTAGE REGULATORS HAD FAILED INTERNALLY & BOTH ALTERNATOR CIRCUIT BREAKERS WERE POPPED.

Probable Cause: FAILURE OF THE PILOT TO PERFORM THE EMERGENCY GEAR EXTENSION PROCEDURE TO ASSURE THAT THE GEAR WAS DOWN AND LOCKED. FACTORS RELATED TO THE ACCIDENT WERE: LOW OIL PRESSURE IN THE RIGHT ENG, FAILURE OF BOTH VOLTAGE REGULATORS, AND THE LOW LEVEL OF CHARGE IN THE BATTERY.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: MIA90LA029
Status: Investigation completed
Duration: 2 years and 8 months
Download report: Final report

Sources:

NTSB MIA90LA029

Location

Revision history:

Date/timeContributorUpdates
22-Mar-2024 17:51 ASN Update Bot Added

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