ASN Wikibase Occurrence # 367993
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Sunday 17 September 1989 |
Time: | 12:54 LT |
Type: | Mooney M20E |
Owner/operator: | Private |
Registration: | N9462V |
MSN: | 700036 |
Year of manufacture: | 1969 |
Total airframe hrs: | 1442 hours |
Engine model: | LYCOMING IO-360-A1A |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Brenham, TX -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Porter, TX (9XS2) |
Destination airport: | Pecos, TX (KPEQ) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:DURING CRUISE AT 6500 FT, OIL APPEARED ON THE WINDSCREEN. FORWARD VISIBILITY WAS SOON RESTRICTED & SEVERE VIBRATIONS PROMPTED THE PLT TO SECURE THE ENG. SUBSEQUENTLY, THE ACFT WAS DMGD WHEN IT HIT A SMALL TREE & ENCTRD UNEVEN TERRAIN DRG A FORCED LNDG. INV REVEALED A 90 DEG ALUMINUM FITTING ON THE PROP GOVERNOR OIL LINE HAD FAILED WHERE IT ENTERED THE ENG CASE. THE OIL LINE WAS STAINLESS STEEL & ITS MOVEMENT WAS DESIGNED TO BE RESTRAINED BY CLAMPS, WHICH WERE NOT IN PLACE. A SVC INSTRN, ISSUED IN 1986, RCMNDD THAT ALUMINUM FITTINGS BE UPGRADED TO STAINLESS STEEL. A SVC BULLETIN DATED 9/8/89 RELATED TO NUMEROUS 'ENGINE FAILURES DUE TO OIL STARVATION RESULTING FROM BROKEN GOVERNOR LINES.' ACCORDING TO THAT BULLETIN, FAILURE TO RE-INSTALL THE GOVERNOR LINE CLAMPS AFTER MAINT HAD BEEN THE CAUSE OF NUMEROUS ENG FAILURES. MAINT PERSONNEL ACCOMPLISHED BOTH A TOP OVERHAUL & AN ANNUAL INSPN, 50 & 12 HRS, RESPECTIVELY, BFR THE ACDNT.
Probable Cause: IMPROPER MAINTENANCE, IMPROPERLY SECURED OIL LINE TO THE PROPELLER GOVERNOR, FAILURE OF THE PROPELLER GOVERNOR OIL LINE, AND SUBSEQUENT LOSS OF OIL, WHICH RESULTED IN OIL EXHAUSTION. FACTORS RELATED TO THE ACCIDENT WERE: FAILURE OF MAINTENANCE PERSONNEL TO FOLLOW THE SERVICE BULLETIN/INSTRUCTION, AND THE TREE AND ROUGH TERRAIN IN THE EMERGENCY LANDING AREA.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW89LA167 |
Status: | Investigation completed |
Duration: | 2 years and 10 months |
Download report: | Final report |
|
Sources:
NTSB FTW89LA167
Location
Revision history:
Date/time | Contributor | Updates |
23-Mar-2024 06:02 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation