ASN Wikibase Occurrence # 36809
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Date: | Tuesday 6 February 1990 |
Time: | 15:48 |
Type: | Piper PA-46-350P Malibu Mirage |
Owner/operator: | private |
Registration: | N8888M |
MSN: | 4622091 |
Total airframe hrs: | 62 hours |
Engine model: | LYCOMING TIO-540-AE2A |
Fatalities: | Fatalities: 2 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Bakersfield, CA -
United States of America
|
Phase: | En route |
Nature: | Executive |
Departure airport: | Porterville, CA (PTV) |
Destination airport: | Redlands, CA (L12) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:BFR TKOF, PLT WAS ADZ OF IFR CONDS ALONG 1ST PART OF ROUTE, WITH FLT PRCTNS FOR OCNL MOD TURBC BLO 15,000' & MIXED ICG FM FRZG LVL (6000') TO 18,000'. HE FILED IFR FLT PLAN WITH CRUISE ALT OF 11,000'. DRG DEP, PLT WAS CLRD TO CLIMB TO 9000' & TOLD TO EXPECT CLNC TO 11,000', 5 MIN LTR . RADAR DATA SHOWED, ACFT CLIMBED AT ABT 1500'/MIN & 100 KTS, SLOWING SLIGHTLY ABV 8000'. AT ABT 9000', ACFT STARTED TO LVL & ACCELERATE. IT THEN CLIMBED MOMENTARILY, DEVIATED LATERALLY FM COURSE & ENTERED STEEP DSCNT. IN-FLT BREAKUP OCCURRED & WRECKAGE WAS SCATTERED over 4100' AREA. TRAJECTORY STUDY SHOWED BREAKUP OCCURRED BTN 4500' & 6500' AS ACFT WAS IN STEEP DSCNT IN EXCESS OF 266 KTS. METALLURGICAL EXAM OF WINGS & STA- BILIZERS REVEALED FEATURES TYPICAL OF OVERSTRESS SEPN; NO PREEXISTING CRACKS OR DEFECTS WERE FND. THE ACFT WAS RECENTLY PURCHASED. PLT'S SON INDCD PRINCIPAL PRBLM WAS 'TWENTY YEAR LEAP IN TECHNOLOGY' FM PREVIOUSLY OWNED PA-24, THAT PLT HAD DIFFICULTY WITH AVIONICS & FLT DRCTR/AUTOPLT, & THAT HE LACKED DETAIL TRNG IN AUTOPLT EMERGENCIES. (SEE:NTSB/SIR-92/03) CAUSE: THE PILOT'S FAILURE TO ACTIVATE THE PITOT HEAT BEFORE FLYING AT AND ABOVE THE FREEZING LEVEL IN INSTRUMENT METEOROLOGICAL CONDITIONS (IMC), FOLLOWED BY HIS IMPROPER RESPONSE TO ERRONEOUS AIRSPEED INDICATIONS THAT RESULTED FROM BLOCKAGE OF THE PITOT TUBE BY ATMOSPHERIC ICING. CONTRIBUTING TO THE ACCIDENT WAS SPATIAL DISORIENTATION OF THE PILOT.
Sources:
NTSB:
https://www.ntsb.gov/ntsb/brief.asp?ev_id=20001212X22579 Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:23 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
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