ASN Wikibase Occurrence # 368649
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Date: | Sunday 4 June 1989 |
Time: | 11:43 LT |
Type: | Beechcraft A24R |
Owner/operator: | Capital City Air Service, Inc. |
Registration: | N9700Q |
MSN: | MC-59 |
Engine model: | LYCOMING IO-360-A1B |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Gulfport, MS -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Pensacola, FL (KPNS) |
Destination airport: | Baton Rouge, LA (BTR |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:WHILE CRUISING IN VFR CONDS ON AN IFR FLT PLAN, THE ENG FAILED & THE PLT ELECTED TO LAND ON A ROAD. AS HE WAS MAKING AN APCH TO LAND, THE ACFT COLLIDED WITH A POWER LINE & A TREE. AN EXAM OF THE ENG REVEALED THE #2 CONNECTING ROD ASSEMBLY HAD FAILED & THE #2 CYLINDER HAD SUBSEQUENTLY SEPARATED. ACCORDING TO THE ACFT OWNER, THE ACFT HAD PREVIOUSLY BEEN INVOLVED IN A SUDDEN ENG STOPPAGE AFTER THE NOSE GEAR HAD COLLAPSED. THE ENG WAS THEN OVERHAULED. AFTER ABOUT ANOTHER 15 HRS OF OPN, THE NOSE GEAR COLLAPSED AGAIN. SUBSEQUENTLY, A DIE PENETRANT CHECK & RUNOUT OF THE CRANKSHAFT FLANGE WAS MADE. ACCORDING TO THE ENG MANUFACTURER, THE INSTALLED CONNECTING RODS & BEARINGS DID NOT CONFORM TO LYCOMING SVC BULLETING #439, DATED 2/17/79. THE ACFT HAD BEEN OPERATED SOME 200 TO 300 HRS SINCE THE LAST ENG OVERHAUL (FOLLOWING THE 1ST GEAR COLLAPSE).
Probable Cause: FAILURE OF A #2 CONNECTING ROD ASSEMBLY, WHICH RESULTED IN SEPARATION OF THE #2 CYLINDER AND SUBSEQUENT LOSS OF ENGINE POWER. CONTRIBUTING FACTORS WERE: INADEQUATE MAINTENANCE, THE TRANSMISSION (POWER) LINE, AND TREES.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA89LA168 |
Status: | Investigation completed |
Duration: | 1 year and 3 months |
Download report: | Final report |
|
Sources:
NTSB MIA89LA168
Location
Revision history:
Date/time | Contributor | Updates |
23-Mar-2024 20:41 |
ASN Update Bot |
Added |
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