ASN Wikibase Occurrence # 368744
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Date: | Sunday 21 May 1989 |
Time: | 16:00 LT |
Type: | Cessna 175 |
Owner/operator: | Private |
Registration: | N7557M |
MSN: | 55857 |
Year of manufacture: | 1959 |
Total airframe hrs: | 2636 hours |
Engine model: | CONTINENTAL GO-300-A |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Sheridan, WY -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | (KSHR) |
Destination airport: | Brule, NE (43V) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PLT RPRTD THAT AFTER TAKEOFF, THE ENG WAS NOT DEVELOPING SUFFICIENT POWER TO CLIMB OR RETURN TO THE AIRPORT. SUBSEQUENTLY, HE FLEW DOWN A CANYON & LANDED IN A HAY FIELD. DRG THE LANDING ROLL, THE ACFT HIT AN UNSEEN DITCH & THE NOSE GEAR COLLAPSED. AN EXAM OF THE ENG REVEALED THAT THE #4 EXHAUST VALVE WAS STICKING. ELEVATION OF THE ARPT WAS 4012 FT.
Probable Cause: BINDING (STUCK) #4 EXHAUST VALVE. HIGH VEGETATION (HAY) AND A HIDDEN OBSTRUCTION (DITCH) WERE CONTRIBUTING FACTORS.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | DEN89LA122 |
Status: | Investigation completed |
Duration: | 1 year |
Download report: | Final report |
|
Sources:
NTSB DEN89LA122
Location
Revision history:
Date/time | Contributor | Updates |
24-Mar-2024 07:02 |
ASN Update Bot |
Added |
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