Accident Aerospatiale AS350D N6003S,
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ASN Wikibase Occurrence # 368751
 
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Date:Saturday 20 May 1989
Time:17:00 LT
Type:Silhouette image of generic AS50 model; specific model in this crash may look slightly different    
Aerospatiale AS350D
Owner/operator:Papillion Helicopters
Registration: N6003S
MSN: 1552
Total airframe hrs:2203 hours
Engine model:LYCOMING LTS-101
Fatalities:Fatalities: 0 / Occupants: 7
Aircraft damage: Substantial
Category:Accident
Location:Waialae Falls, HI -   United States of America
Phase: Manoeuvring (airshow, firefighting, ag.ops.)
Nature:Unknown
Departure airport:Princeville, HI (HPV)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
THE ON-DEMAND AIR TAXI HELICOPTER WAS ON A LOCAL SIGHTSEEING FLT TO WAIALAE FALLS WITH SIX PAX ABOARD. ELEVATION OF THE FALLS WAS ABOUT 3000 FT. AFTER HOVERING AT LOW ALT NEAR THE FALLS, THE PLT BEGAN A PEDAL TURN & BEGAN FORWARD MOVEMENT FOR THE INITIAL CLIMB AWAY FROM THE FALLS. THE MAIN ROTOR RPM DECAYED & THE PLT TURNED BACK TOWARD THE UPPER FALLS, WHERE HE THOUGHT HE COULD LAND. HOWEVER, THE HELICOPTER SETTLED INTO A RAVINE, IMPACTED ROCKS & CAME TO REST. AN EXAM OF THE ENG FUEL CONTROL REVEALED THE MAXIMUM STOP WAS SET AT 93% VERSUS 99% AS SPECIFIED BY THE MANUFACTURER. ALSO, THE GOVERNOR BREAK WAS SET 400 RPM EARLY, THERE WAS NO SEAL ON THE METERING VALVE SLEEVE & THE SAFETY WIRE THRU THE GOVERNOR ADJUSTMENT HAD BEEN CUT & NOT REPLACED.

Probable Cause: IMPROPER MAINTENANCE/ADJUSTMENT OF THE ENGINE FUEL CONTROL UNIT BY COMPANY MAINTENANCE PERSONNEL, WHICH RESULTED IN A SLIGHT LOSS OF ENGINE POWER, AND FAILURE OF THE PILOT TO MAINTAIN ROTOR RPM, WHILE TURNING AND TAKING OFF FROM A HOVER WITH A RELATIVELY HEAVY GROSS WEIGHT. FACTORS RELATED TO THE ACCIDENT WERE: THE HIGH DENSITY ALTITUDE AND ROUGH/UNEVEN (ROCKY) TERRAIN IN THE EMERGENCY LANDING AREA.

Accident investigation:
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Investigating agency: NTSB
Report number: LAX89LA197
Status: Investigation completed
Duration: 1 year and 11 months
Download report: Final report

Sources:

NTSB LAX89LA197

Location

Revision history:

Date/timeContributorUpdates
24-Mar-2024 07:03 ASN Update Bot Added

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