ASN Wikibase Occurrence # 36899
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Date: | Tuesday 20 February 1996 |
Time: | 12:45 LT |
Type: | Beechcraft A36 Bonanza |
Owner/operator: | Flight Enterprises Inc. |
Registration: | N2TC |
MSN: | E-359 |
Year of manufacture: | 1972 |
Total airframe hrs: | 9119 hours |
Engine model: | Continental IO-520-BA |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Katy, TX -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | San Antonio, TX (KSAT) |
Destination airport: | Houston, TX (KIWS) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:After 35 minutes of uneventful flight at 5,500 feet MSL, the pilot contacted ATC to request a lower altitude due to 'not feeling very well.' During the next 45 minutes of flight inbound to his destination airport, he relayed to ATC controllers that he was feeling progressively worse. About 9 miles west of his destination, his radio transmissions were becoming increasingly labored, and he stated that he was 'in bad shape' and was experiencing 'blurred vision.' Subsequent to radar contact being lost, a pilot from another airplane witnessed the aircraft 'swerving back and forth very low to the ground.' He reported that the aircraft impacted the ground 'at cruise speed or faster.' Autopsy findings did not reveal evidence of a cardiac event. Toxicology tests for alcohol and carbon monoxide were negative. An inspection of the aircraft's heater and muffler systems did not reveal any defects. No hazardous or toxic materials were found within the wreckage. The cause of death was determined to be blunt force trauma to the head and chest. The pilot was not wearing a shoulder harness (not installed). After impact damage, there was occupiable volume within the forward cabin structure.
Probable Cause: a loss of control due to pilot incapacitation for undetermined reasons. A factor related to the pilot's injuries was the lack of shoulder harness restraint.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW96FA120 |
Status: | Investigation completed |
Duration: | 1 year and 6 months |
Download report: | Final report |
|
Sources:
NTSB FTW96FA120
Location
Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:23 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
09-Apr-2024 08:10 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Phase, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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