ASN Wikibase Occurrence # 369393
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Thursday 22 December 1988 |
Time: | 10:30 LT |
Type: | Cessna 175 |
Owner/operator: | Private |
Registration: | N7159M |
MSN: | 55459 |
Total airframe hrs: | 3075 hours |
Engine model: | CONTINENTAL GO-300-A |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Lawrence, KS -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | |
Destination airport: | Huntingburg, IN (HNB |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PLT SAID THAT SHORTLY AFTER TAKEOFF, THE ENGINE BEGAN TO MISFIRE AND LOSE POWER. HE ELECTED TO ABORT THE TAKEOFF, BUT WAS UNABLE TO STOP ON THE REMAINING PORTION OF THE RUNWAY. HE RAN OFF THE END, INTO A FARM FIELD, WHERE THE ACFT NOSED DOWN AND WAS SUBSTANTIALLY DAMAGED. THE PLT SAID HE MADE AN INTERSECTION TAKEOFF WHICH GAVE HIM ABOUT 3000 FEET USEABLE RUNWAY INSTEAD OF THE FULL LENGTH OF 5000 FEET. INVESTIGATION REVEALED BOTH SPARK PLUGS ON NO. 3 CYLINDER TO BE MALFUNCTIONING. ONE WAS COMPLETELY DEAD AND THE OTHER FIRED INTERMITTENTLY.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MKC89LA045 |
Status: | Investigation completed |
Duration: | 9 months |
Download report: | Final report |
|
Sources:
NTSB MKC89LA045
Location
Revision history:
Date/time | Contributor | Updates |
24-Mar-2024 14:04 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation