ASN Wikibase Occurrence # 369397
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Tuesday 20 December 1988 |
Time: | 18:45 LT |
Type: | Beechcraft A36 |
Owner/operator: | Bonanza Five, Inc. |
Registration: | N17696 |
MSN: | E1004 |
Total airframe hrs: | 3330 hours |
Engine model: | CONTINENTAL IO-520-BA |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Athens, GA -
United States of America
|
Phase: | En route |
Nature: | Executive |
Departure airport: | Augusta, GA (KDNL) |
Destination airport: | Chamblee, GA (KPDK) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:WHILE CRUISING AT 6,000', THE PLT FELT AN INTENSE VIBRATION FM THE ENG. POWER WAS REDUCED & A DESCENT WAS BEGUN TOWARD A NEARBY ARPT. BEFORE REACHING THE ARPT, THE ENG LOST POWER & AN EMERGENCY WHEELS-UP LANDING WAS MADE IN AN OPEN FIELD. AN EXAM OF THE ENG REVEALED THE #1 EXHAUST VALVE HAD FAILED. THE VALVE GUIDE WAS BATTERED & BROKEN, AND WAS LOOSE IN ITS BORE. THE BORE WAS FRETTED & HAD BECOME OVERSIZED. THE ENG HAD BEEN OVERHAULED & INSTALLED IN THE ACFT ON 1/20/82 WITH A TOTAL TIME OF 1515 HRS. ACCORDING TO THE LOG BOOK, NEW VALVES & VALVE GUIDES HAD BEEN INSTALLED AT THAT TIME. THE ENG TIME SINCE MAJOR OVERHAUL WAS 1041 HRS.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ATL89LA056 |
Status: | Investigation completed |
Duration: | 11 months |
Download report: | Final report |
|
Sources:
NTSB ATL89LA056
Revision history:
Date/time | Contributor | Updates |
24-Mar-2024 14:10 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation