ASN Wikibase Occurrence # 369656
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 15 October 1988 |
Time: | 15:35 LT |
Type: | Beechcraft 35 |
Owner/operator: | C & D Airforo, Inc. |
Registration: | N4553V |
MSN: | D-1381 |
Year of manufacture: | 1948 |
Engine model: | CONTINENTAL E-225-8 |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Tampa, FL -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | (KMCF) |
Destination airport: | St. Petersburg, FL (CLW |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PLT STATED THE ACFT WAS TOPPED WITH 30 GALS OF AUTO FUEL PRIOR TO DEPARTING FOR THE OPEN HOUSE AT MCDILL AFB. THE FLT TO MCDILL WAS NORMAL. BEFORE DEPARTURE, ABOUT 1/2 INCH OF WATER WAS DRAINED FROM THE FUEL SYSTEM DURING PREFLT INSPECTION. AT ABOUT 300 FT IMMEDIATELY AFTER TAKEOFF, THE ENGINE QUIT & THE PLT MADE A FORCED LDG INTO A FIELD WHERE THE RT WING OF THE ACFT HIT A POLE AS IT SLID ALONG ON THE BELLY. THE ENGINE WAS SUBSEQUENTLY TEST-RUN SATISFACTORILY.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA89LA011 |
Status: | Investigation completed |
Duration: | 1 year |
Download report: | Final report |
|
Sources:
NTSB MIA89LA011
Revision history:
Date/time | Contributor | Updates |
24-Mar-2024 16:53 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation