ASN Wikibase Occurrence # 370022
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Date: | Saturday 13 August 1988 |
Time: | 15:10 LT |
Type: | Champion 7KCAB |
Owner/operator: | Private |
Registration: | N5124T |
MSN: | 23 |
Year of manufacture: | 1967 |
Engine model: | LYCOMING IO-320 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Grand Haven, MI -
United States of America
|
Phase: | En route |
Nature: | Executive |
Departure airport: | Grand Haven, MI (3GM |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PILOT STATED THAT HE WAS TOWING BANNERS ON THE DAY OF THE ACCIDENT. AFTER TOWING THE THIRD BANNER FOR AN ESTIMATED 1 1/4 HOURS, HE WAS RETURNING TO THE DEPARTURE AIRPORT WHEN THE AIRCRAFT'S ENGINE FAILED COMPLETELY. HE SELECTED THE 'CLOSEST FIELD THAT LOOKED THE BEST...' AND EXECUTED A FORCED LANDING ON AN AREA OF ROUGH SAND DUNES. THE PILOT HAD A COMMERCIAL PILOT'S CERTIFICATE WITH APPROXIMATELY 633 HOURS TOTAL FLIGHT TIME, OF WHICH 72 HOURS WERE IN THE ACCIDENT MAKE AND MODEL AIRCRAFT. THE PILOT REPORTED THAT HE HAD BEEN TOWING BANNERS FOR 'TWO SEASONS' AND 'ALWAYS TIMED...FUEL BURN TO LEAVE 1 HOUR RESERVE.' HE STATED THAT HE JUDGED HIS FUEL QUANTITY BY THE CUMULATIVE HOURS THE AIRCRAFT HAD FLOWN SINCE THE AIRCRAFT HAD NO ELECTRIC FUEL QUANTITY INDICATOR. HE STATED THAT HE ESTIMATED THAT HE HAD ONE HOUR OF FUEL REMAINING WHEN THE ENGINE QUIT.
Probable Cause: THE PILOT'S INATTENTIVE FUEL SYSTEM MONITORING, AND THE RESULTANT TOTAL FAILURE OF THE AIRCRAFT'S POWERPLANT DUE TO FUEL EXHAUSTION. A FORCED LANDING WAS EXECUTED ON A STRETCH OF BEACH WITH SAND DUNES, AND THE AIRCRAFT WAS SUBSTANTIALLY DAMAGED DURING THE ROUGH TOUCHDOWN AND LANDING ROLL. THE PILOT EXPECTED TO HAVE AT LEAST ANOTHER HOUR OF FUEL, BASED ON PREVIOUS EXPERIENCE. FUEL QUANTITY WAS BEING JUDGED BY TIMING THE DURATION OF ACCUMULATED FLIGHTS; NO ELECTRIC FUEL QUANTITY INDICATOR WAS INSTALLED.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI88DEM08 |
Status: | Investigation completed |
Duration: | 2 years and 2 months |
Download report: | Final report |
|
Sources:
NTSB CHI88DEM08
Location
Revision history:
Date/time | Contributor | Updates |
24-Mar-2024 20:47 |
ASN Update Bot |
Added |
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