Serious incident Boeing 737-790 N614AS,
ASN logo
ASN Wikibase Occurrence # 370277
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Thursday 19 October 2006
Time:01:00 LT
Type:Silhouette image of generic B737 model; specific model in this crash may look slightly different    
Boeing 737-790
Owner/operator:Alaska Airlines
Registration: N614AS
MSN: 30343/439
Year of manufacture:1999
Engine model:General Electric CFM56SER
Fatalities:Fatalities: 0 / Occupants: 5
Aircraft damage: None
Category:Serious incident
Location:Los Angeles, CA -   United States of America
Phase: En route
Nature:Unknown
Departure airport:Los Angeles International Airport, CA (LAX/KLAX)
Destination airport:MMX
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
During cruise flight, just after entry into foreign airspace, the flight crew was alerted to a System B hydraulic failure, and they decided to return to, and land in the United States (US). Upon re-entry to US airspace, the flight crew declared an emergency and requested to land at the departure airport. On final approach, about 5 minutes after selecting flaps to 15 and lowering the landing gear, the flight crew was alerted to the System A hydraulic quantity gage, that had dropped to 0 pounds per square inch (psi). At this point both System A LOW PRESSURE LIGHTS illuminated and the airplane went into the manual reversion mode. The flight crew indicated that the airplane was difficult to control; however, they landed uneventfully at the airport. Maintenance personnel for the airline, and the airplane manufacturer, inspected the hydraulic systems. They noted that the initiating event was a failed engine driven pump. The secondary event was a cracked hydraulic line that failed due to fatigue. A metallurgical examination revealed the fatigue fracture initiated at the toe of the welding root where they were able to locate a crack that had propagated through half the perimeter. The airframe manufacturer redesigned the affected tube, part number 272A4451-87, a titanium tube, with part number 272A4451-200, a stainless steel tube.

Probable Cause: A complete failure and depressurization of both hydraulic systems due to two separate events: 1) the failure of a engine driven pump on the 'A' system, and 2) the fatigue fracture and failure of a hydraulic line on the 'B' system.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX07IA014
Status: Investigation completed
Duration: 1 year and 5 months
Download report: Final report

Sources:

NTSB LAX07IA014

Revision history:

Date/timeContributorUpdates
25-Mar-2024 08:56 ASN Update Bot Added

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org