ASN Wikibase Occurrence # 370393
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Date: | Tuesday 5 August 2003 |
Time: | 11:20 LT |
Type: | Cessna 402C |
Owner/operator: | Air Florida Express |
Registration: | N371R |
MSN: | 0028 |
Total airframe hrs: | 15303 hours |
Engine model: | Teledyne Continental TSIO-520 VB |
Fatalities: | Fatalities: 0 / Occupants: 4 |
Aircraft damage: | None |
Category: | Serious incident |
Location: | Arecibo, PR -
Puerto Rico
|
Phase: | En route |
Nature: | Unknown |
Departure airport: | Fort Lauderdale International Airport, FL (FLL/KFLL) |
Destination airport: | STT |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot stated that while at an altitude of 9,500 feet, in the vicinity of Grand Turk, he noticed the airplane's fuel gauges fluctuating over a 60 gallon range. He said he continued the flight with confidence in his flight planning, and about 40 nautical miles from Isla Grande Airport the right engine sputtered. The pilot said he turned the fuel pumps on, checked the fuel pressure, and noted zero on the fuel quantity indicator, so he selected fuel from the left tank. He said he was also reading a low pressure for the left engine. After climbing to 11,500 feet, about 35 miles from Isla Grande Airport the left engine ceased operating. The right engine then ceased operating a short time after, and the pilot said he feathered both propellers, declared an emergency, and diverted to the Arecibo Airport. He then switched the fuel selector from left tank to right tank, and was able to restart the right engine, and fly toward the shore, and then the right engine ceased operating. About two nautical miles north of the Arecibo Airport, at 6,000 feet and descending, the pilot said he got the left engine operating again. He said he then extended the landing gear, entered a right crosswind, extended full flaps on a right downwind, and landed on runway 08. After off-loading his passengers, the pilot said he was debriefed by an FAA inspector, who issued him a ferry permit to operate the airplane. The pilot then purchased fuel and ferried the airplane to Borinquen Airport where he "topped the tanks" with additional fuel.
Probable Cause: The pilot's inadequate in-flight decision, and his failure to refuel, which led to fuel exhaustion and subsequent loss of engine power.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA03IA157 |
Status: | Investigation completed |
Duration: | 8 months |
Download report: | Final report |
|
Sources:
NTSB MIA03IA157
Location
Revision history:
Date/time | Contributor | Updates |
25-Mar-2024 10:14 |
ASN Update Bot |
Added |
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