ASN Wikibase Occurrence # 370517
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Date: | Wednesday 3 January 2001 |
Time: | 10:32 LT |
Type: | Bombardier CRJ-100ER |
Owner/operator: | Comair |
Registration: | N933CA |
MSN: | 7040 |
Total airframe hrs: | 16298 hours |
Engine model: | GE CF34-3A1 |
Fatalities: | Fatalities: 0 / Occupants: 46 |
Aircraft damage: | Minor |
Category: | Serious incident |
Location: | Covington, KY -
United States of America
|
Phase: | Approach |
Nature: | Passenger - Scheduled |
Departure airport: | Minneapolis-St. Paul International Airport, MN (MSP/KMSP) |
Destination airport: | Cincinnati/Northern Kentucky Airport, KY (CVG/KCVG) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During climbout, an airframe vibration developed. All gauges, readouts, synoptic pages, and airplane controls were normal. The crew contacted their maintenance base and attempted to troubleshoot the problem, but could not determine its cause. The vibration remained unchanged until the airplane leveled off at 7,000 feet during an approach. At that time, the crew felt a bump, then the vibration completely ceased. The airplane landed, and taxied to the gate without further incident. Post-flight inspection revealed that the number 1 exhaust fairing was missing, and that the left, aft fuselage had a dent. The 30 bolts that would have normally attached the exhaust nozzle assembly to the exhaust frame were all missing, "without a trace." Seven months earlier, the tailpipe was found loose. Ten bolts were replaced, and the rest were re-torqued. The last inspection on the airplane had been completed about 2 weeks earlier, 105 hours prior to the incident. Company personnel had previously found cracked bolts on exhaust flanges from other engines. Laboratory examination of used bolts from another engine revealed no anomalies. Engine shop buildup and shop exit manuals were subsequently revised to make the installation and torquing of exhaust nozzle bolts a required inspection item.
Probable Cause: Missing exhaust nozzle bolts for undetermined reasons. A factor was inadequate maintenance inspection of the affected area.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | NYC01IA072 |
Status: | Investigation completed |
Duration: | 12 months |
Download report: | Final report |
|
Sources:
NTSB NYC01IA072
Location
Revision history:
Date/time | Contributor | Updates |
25-Mar-2024 11:32 |
ASN Update Bot |
Added |
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