ASN Wikibase Occurrence # 370674
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Date: | Sunday 17 July 1988 |
Time: | 09:45 LT |
Type: | Mooney M20F |
Owner/operator: | Leo Otway |
Registration: | N6310Q |
MSN: | 670403 |
Year of manufacture: | 1967 |
Total airframe hrs: | 3249 hours |
Engine model: | LYCOMING IO-360-A1A |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Princeton, NJ -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE MOONEY M20F MADE A TAKEOFF AND AS THE PILOT TURNED CROSSWIND, HE EXPERIENCED A PARTIAL POWER LOSS. HE RETURNED FOR A LANDING AND THE ENGINE SMOOTHED OUT. HE MADE EXTENSIVE GROUND RUNS AND COULD NOT DUPLICATE THE PROBLEM. HOWEVER HE DID NOT HAVE MAINTENANCE PERSONNEL LOOK AT THE AIRCRAFT. ON THE SECOND TAKEOFF, HE AGAIN LOST POWER AND THIS TIME, MADE AN OFF AIRPORT LANDING IN A FIELD. EXAMINATION OF THE ENGINE REVEALED THAT THE SPARK PLUGS HAD SOOT ON THEM. THE FUEL INJECTOR SERVO, MANIFOLD, AND NOZZLES CHECKED OUT OK; HOWEVER, THE RUBBER INTAKE BOOT BETWEEN THE AIR FILTER AND THE FUEL SERVO WAS FOUND PARTIALLY COLLAPSED.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | NYC88LA184 |
Status: | Investigation completed |
Duration: | 1 year and 6 months |
Download report: | Final report |
|
Sources:
NTSB NYC88LA184
Revision history:
Date/time | Contributor | Updates |
25-Mar-2024 13:41 |
ASN Update Bot |
Added |
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