ASN Wikibase Occurrence # 370981
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Date: | Sunday 5 June 1988 |
Time: | 12:30 LT |
Type: | Beechcraft C23 |
Owner/operator: | Private |
Registration: | N9311S |
MSN: | M 1634 |
Total airframe hrs: | 3634 hours |
Engine model: | LYCOMING O-360-A4K |
Fatalities: | Fatalities: 0 / Occupants: 4 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Gallup, NM -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | |
Destination airport: | Amarillo, TX |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PRIVATE PLT WAS TAKING OFF WITH THREE PASSENGERS FOR A PERSONAL TRANSPORTATION FLIGHT. THE AIRPLANE LEFT THE RUNWAY AND ONLY GAINED ABOUT 50 FEET AGL ACCORDING TO A WITNESS. THE PLT REPORTED THAT THE AIRCRAFT REACHED 200 FEET AGL. THE AIRPLANE STALLED AND FELL BACK ON THE RUNWAY, THE RIGHT WING STRUCK THE RUNWAY FIRST AND THE LANDING GEAR WAS SHEARED OFF. THE AIRPLANE CAME TO REST OFF THE RUNWAY. THE DESITY ALTITUDE WAS REPORTED BY THE FSS AS 9,200 FEET. THE PILOT STATED THAT HIS AIRPLANE WAS LOADED TO WITHIN 20 POUNDS OF THE MAXIMUM ALLOWABLE GROSS WEIGHT. THE PLT ALSO SAID THAT HE HAD NOT LEANED THE MIXTURE PROPERLY AND FELT THAT THE ENGINE WAS NOT PRODUCING FULL POWER.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | DEN88LA122 |
Status: | Investigation completed |
Duration: | 1 year 1 month |
Download report: | Final report |
|
Sources:
NTSB DEN88LA122
Location
Revision history:
Date/time | Contributor | Updates |
25-Mar-2024 16:49 |
ASN Update Bot |
Added |
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