ASN Wikibase Occurrence # 371160
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 7 May 1988 |
Time: | 13:25 LT |
Type: | Hughes 269B |
Owner/operator: | Warner Aviation |
Registration: | N9487F |
MSN: | 270313 |
Year of manufacture: | 1967 |
Total airframe hrs: | 2230 hours |
Engine model: | LYCOMING HIO-360-A1A |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Minneapolis, MN -
United States of America
|
Phase: | Initial climb |
Nature: | Executive |
Departure airport: | Behtel College, MN |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PILOT WAS EXECUTING A DOWNWIND TAKEOFF, THE WINDS REPORTEDLY GUSTING TO 25 KNOTS, LOADED WITH TWO PASSENGERS, WHEN JUST AFTER TAKEOFF THE PILOT STATED THE HELICOPTER EXPERIENCED A LOSS OF POWER. THE PILOT THEN ATTEMPTED TO EXECUTE AN AUTOROTATION, BUT DURING THE EMERGENCY DESCENT THE PILOT WAS UNABLE TO MAINTAIN DIRECTIONAL CONTROL. AS A RESULT THE HELICOPTER STRUCK A MOVING VEHICLE WITH ITS TAIL ROTOR AND SUBSEQUENTLY COLLIDED WITH THE TERRAIN. THE HELICOPTER WAS APPROXIMATELY 130 LBS UNDER GROSS WT AT THE TIME OF TAKEOFF. WHEN EXAMINED AND TESTED THE ENGINE OPERATED NORMALLY AND NO MECHANICAL MALFUNCTIONS WERE FOUND. EXAMINATION OF THE ENGINE DID REVEAL THAT A FUEL NOZZLE HAD BEEN INSTALLED IN THE AIRCRAFT'S FUEL SYSTEM WITH A RESTRICTOR MISSING BUT TO COMPENSATE FOR THE MISSING RESTRICTOR THE FUEL SERVO IDLE MIXTURE WAS SET AT A VERY LEAN SETTING. THIS WAS DETERMINED NOT TO BE A FACTOR IN THE ACCIDENT.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI88LA108 |
Status: | Investigation completed |
Duration: | 1 year 1 month |
Download report: | Final report |
|
Sources:
NTSB CHI88LA108
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
25-Mar-2024 18:35 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation