ASN Wikibase Occurrence # 371188
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Date: | Sunday 1 May 1988 |
Time: | 15:44 LT |
Type: | Boeing Stearman A75-N1 |
Owner/operator: | Private |
Registration: | N53125 |
MSN: | 75-1773 |
Total airframe hrs: | 5392 hours |
Engine model: | P&W R-985-AN3 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Medford, OR -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Private |
Departure airport: | Medford, OR (KMFR) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:PLT PERFORMED A NEGATIVE 'G' MANEUVER, ESTIMATED AT 2 TO 2.5 NEGATIVE 'G' FORCE, FOLLOWING WHICH THE ENGINE LOST POWER. A FORCED LANDING WAS ACCOMPLISHED IN SCRUB TREES. THE ENGINE IS EQUIPPED WITH A FLOAT CARBURETOR. THERE WERE INDICATIONS THAT THE CAUSE OF POWER LOSS WAS NEGATIVE 'G' DISPLACEMENT OF ONE OR BOTH FLOATS IN THE CARBURETOR BOWL (STUCK FLOAT), RESULTING IN FUEL STARVATION.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | SEA88LA087 |
Status: | Investigation completed |
Duration: | 10 months |
Download report: | Final report |
|
Sources:
NTSB SEA88LA087
Location
Revision history:
Date/time | Contributor | Updates |
25-Mar-2024 18:55 |
ASN Update Bot |
Added |
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