Serious incident McDonnell Douglas DC-10-40 N154US,
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ASN Wikibase Occurrence # 371339
 
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Date:Wednesday 30 March 1988
Time:20:30 LT
Type:Silhouette image of generic DC10 model; specific model in this crash may look slightly different    
McDonnell Douglas DC-10-40
Owner/operator:Northwest Airlines
Registration: N154US
MSN: 46763/128
Total airframe hrs:33818 hours
Engine model:P&W JT9D-20
Fatalities:Fatalities: 0 / Occupants: 86
Aircraft damage: Minor
Category:Serious incident
Location:Boston, MA -   United States of America
Phase: Taxi
Nature:Passenger - Scheduled
Departure airport:New York-John F. Kennedy International Airport, NY (JFK/KJFK)
Destination airport:(KBOS)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
DRG TAXI TO GATE AFTER LDG, CREW STARTED APU NORMALLY. WHILE TAXIING NR 3 PNEUMATIC DUCT FAIL LT ILLUMINATED. LATER, THE CENTER ACCESSORY COMPT (CAC) DOOR WARNING LT ILLUMINATED AND GND PERS SAW SMOKE EMANATING FM THE FUSELAGE OUTFLOW VALVES. AFTER ENG SHUTDOWN, SMOKE ENTERED THE CABIN AND THE APU TRIPPED OFF. FIRE DEPT PERS FND CAC OUTSIDE DOOR HOT, THEN, USING CABIN FLOOR HATCH, OBSRVED 1-2 FT HIGH FLAMES IN CAC. FIRE WAS EXTINGUISHED WITH DMG LIMITED TO CAC. INVEST REVEALED IMPROPER/LOOSE BATTERY GND CONNECTION. NORMAL CABLE MOVEMENT WOULD LOOSEN CONNECTION DRG BATT DISCONNECT. BURNED INSULATION BLANKETS MET SPEC BUT WERE COATED WITH SYNTHETIC HYD FLUID (SLAT ACTUATOR LKG) AND JET FUEL. FIRE PATTERN SUGGESTED FUEL SEEPAGE ALONG BULKHEAD FASTENER LINE. BATT GND LAST INSTALLED NOV,87. BATT LAST CHDG 2 WKS BEFORE INCIDENT. SERVICE BULLETIN PERTAINING TO BATT GND NOT COMPLIED. INOPERATIVE CAC DRAIN VALVES ALLOWED FUEL TO POOL IN CAC BILGE. NO CAC FIRE WARNING OR EXTINGUISHER SYSTEM WAS INSTALLED.

Probable Cause: THE IMPROPER INSTALLATION OF THE BATTERY GROUND CONNECTION THAT RESULTED IN PREMATURE LOOSENING OF THE CONNECTION AND ELECTRICAL ARC IGNITION OF POOLED FUEL IN THE CAC BILGE. THE FUEL WAS NOT DRAINED OVERBOARD DUE TO INOPERATIVE CAC BILGE AREA DRAIN VALVES. CONTRIBUTING TO THE INCIDENT WAS NORTHWEST'S NON-COMPLIANCE WITH A SERVICE BULLETIN TO MODIFY THE GROUND CABLE ATTACHMENT BRACKET TO PREVENT LOOSENING OF THE CONNECTION.

Accident investigation:
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Investigating agency: NTSB
Report number: DCA88IA044
Status: Investigation completed
Duration: 1 year and 10 months
Download report: Final report

Sources:

NTSB DCA88IA044

Revision history:

Date/timeContributorUpdates
25-Mar-2024 20:34 ASN Update Bot Added

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