ASN Wikibase Occurrence # 372129
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Sunday 27 September 1987 |
Time: | 10:30 LT |
Type: | Hughes 369D |
Owner/operator: | Private |
Registration: | N8613F |
MSN: | 670127D |
Total airframe hrs: | 3129 hours |
Engine model: | Allison 250-C20B |
Fatalities: | Fatalities: 0 / Occupants: 4 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Seattle, WA -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Sheldon, WA (KSHN) |
Destination airport: | Everett, WA (KPAE) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PLT RPRTD THAT WHILE HE WAS IN CRUISE FLIGHT AT ABOUT 1000', THE ENG LOST POWER. HE INITIATED AN AUTOROTATION TO AN ATHLETIC FIELD IN A CITY PARK. DRG HIS APCH, HE CHANGED HIS PLANNED TOUCHDOWN POINT SVRL TIMES DUE TO PERSONNEL ON THE FIELD. HE SAID THAT THIS RESULTED IN A LOSS OF AIRSPEED, & SUBSEQUENTLY, THE HELICOPTER LANDED HARD. DRG TOUCHDOWN, THE MAIN ROTOR BLADES FLEXED DOWNWARD & SEVERED THE TAIL BOOM. AN EXAM OF THE ENG REVEALED NO EVIDENCE OF A MECHANICAL MALFUNCTION THAT WOULD HAVE RESULTED IN A LOSS OF POWER.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | SEA87FA194 |
Status: | Investigation completed |
Duration: | 1 year and 4 months |
Download report: | Final report |
|
Sources:
NTSB SEA87FA194
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
26-Mar-2024 13:49 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation