ASN Wikibase Occurrence # 372260
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Date: | Monday 7 September 1987 |
Time: | 11:25 LT |
Type: | Piper PA-28-140 |
Owner/operator: | Virgil L.korona |
Registration: | N5581U |
MSN: | 2826312 |
Total airframe hrs: | 2167 hours |
Engine model: | LYCOMING O-320-E2A |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Ocala, FL -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:SHORTLY AFTER TAKEOFF, THE ENG BEGAN TO LOSE PWR & THE PLT WAS UNABLE TO MAINT ALT OR RETURN TO THE ARPT. HE ELECTED TO LAND ON A ROAD, BUT THERE WAS ONCOMING TRAFFIC, SO HE MANEUVERED TO THE LEFT SIDE. SUBSEQUENTLY, THE LEFT WING COLLIDED WITH A UTILITY POLE. ACCORDING TO A WITNESS, THE ACFT WAS SLOW TO CLIMB AFTER TAKEOFF, ALTHOUGH NO UNUSUAL ENG SOUNDS WERE NOTED. AFTER THE ACDNT, AN OPNL CHECK OF THE ENG WAS MADE, BUT WAS LIMITED TO 1650 RPM DUE TO ACDNT DAMAGE. THE SOLE DISCREPANCY NOTED DRG THE ENG RUN WAS A LOOSE GASCOLATOR; HOWEVER, THE INVESTIGATION DID NOT VERIFY WHETHER THE GASCOLATOR HAD LOOSENED BEFORE OR DRG IMPACT.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA87LA241 |
Status: | Investigation completed |
Duration: | 1 year and 4 months |
Download report: | Final report |
|
Sources:
NTSB MIA87LA241
Revision history:
Date/time | Contributor | Updates |
26-Mar-2024 15:17 |
ASN Update Bot |
Added |
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