Serious incident Boeing 727-225 N8892Z,
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ASN Wikibase Occurrence # 372670
 
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Date:Saturday 11 July 1987
Time:18:38 LT
Type:Silhouette image of generic B722 model; specific model in this crash may look slightly different    
Boeing 727-225
Owner/operator:Eastern Air Lines
Registration: N8892Z
MSN: 21861/1554
Year of manufacture:1979
Total airframe hrs:24354 hours
Engine model:P&W JT8D-15
Fatalities:Fatalities: 0 / Occupants: 87
Aircraft damage: Minor
Category:Serious incident
Location:Washington, DC -   United States of America
Phase: Unknown
Nature:Passenger - Scheduled
Departure airport:Orlando International Airport, FL (MCO/KMCO)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
DRG ARR, THE ACFT'S RADAR SHOWED TSTMS IN THE AREA OF THE ARPT. AS THE FLT CONTD, ATIS INFO CHGD. WHEN THE PLTS CTCD WASHINGTON APCH CTL WITH OLD ATIS INFO, THE CTLR DID NOT CORRECT THE FLT. THEY WERE ADZD OF HVY RAIN, STRONG WNDS & A PIREP OF WNDSHR NR THE ARPT, BUT THEY WERE NOT INFORMED THAT THE LOW LVL WNDSHR ALERT SYS (LLWAS) WAS INOP. THE FLT WAS VECTORED FOR A ROSSLYN RWY 18 APCH. AFTER CTCG THE TWR, THE PLTS WERE ADZD THE WND WAS FM 230 DEG AT 35 TO 45 KTS. SHORTLY THEREAFTER, ON FINAL APCH, THE ACFT WAS 'INUNDATED' BY RAIN. THE CREW LOST SIGHT OF THE ARPT, BGN A MISSED APCH (M/A), & ENCTRD LARGE HAIL & MOD TURBC. DRG THE M/A, THE ACFT STOPPED CLBG AT APRX 600' & THE SPEED SLOWED FM 170 TO 138 KTS. THE CAPT APPLIED FULL PWR & THE ACFT RESPONDED, BUT THE N1 & EGT LMTS WERE EXCEEDED. THE CAPT REDUCED PWR & DIVERTED TO DULLES INTL ARPT. A POST FLT EXAM REVEALED THE 1ST & 2ND STAGE TURBINE BLADES OF ALL 3 ENGS HAD BEEN OVERTEMPED.

Probable Cause:

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: MIA87IA204
Status: Investigation completed
Duration: 2 years
Download report: Final report

Sources:

NTSB MIA87IA204

Location

Revision history:

Date/timeContributorUpdates
26-Mar-2024 20:14 ASN Update Bot Added

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