ASN Wikibase Occurrence # 373160
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 25 April 1987 |
Time: | 17:35 LT |
Type: | Cessna 500 Citation I |
Owner/operator: | Firebird Enterprises, Inc. |
Registration: | N82AT |
MSN: | 500-3012 |
Total airframe hrs: | 4553 hours |
Engine model: | P&W JT15D-1 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Willoughby, OH -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | |
Destination airport: | Middlefield, OH (7G8) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:ACFT HAD BEEN FLOWN OVER 4 HRS ON PERS. BUSINESS FOR OWNER. PLTS HAD STOPPED AT LNN TO DROP OFF PAX. START & TAXI WERE NORM FOR POSITIONING FLT BACK TO HOME BASE. STARTED T.O. ROLL AND WHEN ENG RPM REACHED 80-85% TOWARD TGT OF 95.7%, PLTS REPTD LOUD 'BANG' AND CP OBSERVED LEFT ENG FAN STAGE PASS THE ACFT, ARC UP AND TO THE RIGHT, AND THEN STRIKE GND AT THE EDGE OF THE RWY AND BOUNCE ONTO THE GRASS 125 FT RIGHT OF THE RWY. THE PLT STOPPED THE ACFT ON THE RWY. INSP OF THE ACFT AND ENG REVEALED UNCONTAINED FAILURE OF LEFT ENG IMPELLER. INSP OF IMPELLER REVEALED FATIGUE CRACKS ON PRESSURE FACE OF IMPELLER.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ATL87FA124 |
Status: | Investigation completed |
Duration: | 1 year 1 month |
Download report: | Final report |
|
Sources:
NTSB ATL87FA124
Location
Revision history:
Date/time | Contributor | Updates |
27-Mar-2024 10:16 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation