Accident Piper PA-28-161 N114AV,
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ASN Wikibase Occurrence # 37352
 
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Date:Friday 19 January 1996
Time:13:35 LT
Type:Silhouette image of generic P28A model; specific model in this crash may look slightly different    
Piper PA-28-161
Owner/operator:Florida Flyers U K Inc
Registration: N114AV
MSN: 28-7916563
Year of manufacture:1979
Total airframe hrs:7689 hours
Engine model:Lycoming O-320-D3G
Fatalities:Fatalities: 1 / Occupants: 3
Aircraft damage: Substantial
Category:Accident
Location:Fort Pierce, FL -   United States of America
Phase: Initial climb
Nature:Private
Departure airport:(KFPR)
Destination airport:Ft Lauderdale, FL (FLL
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
According to the air traffic controller in the airport tower, about 5,000 feet of the runway was used for the takeoff roll. Witnesses reported that after lift-off, the airplane climbed about 200 to 300 feet above the runway and entered a steep right turn. The nose then dropped, and the airplane collided with the ground, adjacent to the runway. Presumably, due to injury, the pilot was unable to recall the occurrence. During a postaccident examination of the airplane, a foam-like material, used for the carburetor air intake filter, was found lodged in the carburetor throat; and one half of the retaining screen (to hold the foam) was absent. According to the aircraft records, the airplane had received an annual inspection three days before the accident flight, during which the filter was replaced. The airplane had been operated for an unspecified time following the inspection. Piper Service Bulletin 891 had been issued to provide for a one piece retainer for the filter, which would have precluded the filter from being drawn into the induction system.

Probable Cause: improper re-assembly of the engine induction air filter by maintenance personnel, during an annual inspection, which resulted in a loss of engine power during takeoff; failure of the pilot to abort the takeoff before lift-off; and failure of the pilot to obtain and/or maintain sufficient airspeed, which resulted in a stall.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ATL96FA037
Status: Investigation completed
Duration: 8 months
Download report: Final report

Sources:

NTSB ATL96FA037

Location

Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
21-Dec-2016 19:23 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
09-Apr-2024 08:30 ASN Update Bot Updated [Time, Other fatalities, Phase, Departure airport, Destination airport, Source, Narrative, Category, Accident report]

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