ASN Wikibase Occurrence # 373528
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Date: | Saturday 21 February 1987 |
Time: | 15:56 LT |
Type: | Beechcraft A36TC |
Owner/operator: | Private |
Registration: | N47EE |
MSN: | EA-272 |
Total airframe hrs: | 830 hours |
Engine model: | CONTINENTAL TSIO-520-UB |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Orlando, FL -
United States of America
|
Phase: | Take off |
Nature: | Training |
Departure airport: | |
Destination airport: | Melbourne, FL (KMLB) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:DRG THE TAKEOFF ROLL, LGT COLORED SMOKE WAS SEEN TRAILING THE THE ACFT. THE PLT RPRTD THAT AT 100 TO 200 FT AGL, THE ENGLOST PARTIAL PWR. HE SAID HE CHECKED ALL CTLS & RAISED THE LNDG GEAR. WITNESSES RPRTD THAT AT ABOUT THAT TIME, HEAVY SMOKE BGN TRAILING THE ACFT & THE ENG BACKFIRED & QUIT. THE PLT SAID THE SAFETY PLT THEN TOOK CTL & ATMTD TO RETURN TO THE ARPT. AT ABOUT THAT TIME, THE ACFT STALLED, DSCNDD OUT OF CTL & CRASHED AT THE EDGE OF A LAKE. RSN FOR THE INITIAL PWR LOSS WAS NOT DETERMINED. THE ELEC BOOST PUMP WAS FND IN THE HI PSN AFTER THE ACDNT. THE FLT MANUAL WARNED THAT THE HI BOOST PUMP MUST NOT BE USED UNLESS THE ENG DRIVEN FUEL PUMP HAD FAILED; OTHERWISE, INCREASED PRESSURE FM THE HI BOOSTPUMP WOULD RESULT IN ENG ROUGHNESS; IN SOME CASES, ENG COMBUSTION MAY CEASE. THE ENG OPERATED NORMALLY IN A TEST CELL AFTER THE ACDNT. WHEN ANOTHER ENG WAS TESTED, LOSS OF PWR OCCURRED 3 TO 5 SEC AFTER THE HI BOOST PUMP WAS ACTIVATED. ALSO, A CRACK WAS FND IN THE TURBOCHARGER INLET PIPE, BUT DUPLICATION OF THIS RESULTED IN ONLY A MINOR PWR LOSS.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA87FA091 |
Status: | Investigation completed |
Duration: | 1 year and 6 months |
Download report: | Final report |
|
Sources:
NTSB MIA87FA091
Location
Revision history:
Date/time | Contributor | Updates |
27-Mar-2024 14:04 |
ASN Update Bot |
Added |
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