ASN Wikibase Occurrence # 373550
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Tuesday 17 February 1987 |
Time: | 09:00 LT |
Type: | Cessna 150C |
Owner/operator: | Solberg Aviation |
Registration: | N63218 |
MSN: | 15077184 |
Year of manufacture: | 1975 |
Total airframe hrs: | 4897 hours |
Engine model: | CONTINENTAL O-200-A |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Manville, NJ -
United States of America
|
Phase: | Standing |
Nature: | Survey |
Departure airport: | |
Destination airport: | Readington, NJ (N51) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:AFTER MAKING A REST STOP, THE PLT ATTEMPTED TO RESTART THE ENG, USING A NORMAL START PROCEDURE, BUT THE STARTER WOULD NOT ENGAGE. HE TRIED TO TURN OFF THE IGNITION SWITCH, BUT SAID THAT 'POSSIBLY DUE TO THE FACT THAT I WAS WEARING HEAVY GLOVES, I FAILED TO SHUT THE MAG SWITCH OFF COMPLETELY.' HE THEN GOT OUT OF THE ACFT WITH THE INTENTION OF MOVING THE PROP SO THAT THE STARTER WOULD ENGAGE. AS HE MOVED THE PROP 'AN INCH OR TWO,' THE ENG STARTED. SUBSEQUENTLY, THE ACFT STARTED MOVING & COLLIDED WITH TWO OTHER AIRPLANES BEFORE IT CAME TO REST.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | NYC87LA090 |
Status: | Investigation completed |
Duration: | 1 year and 8 months |
Download report: | Final report |
|
Sources:
NTSB NYC87LA090
Revision history:
Date/time | Contributor | Updates |
27-Mar-2024 14:18 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation