ASN Wikibase Occurrence # 373671
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 24 January 1987 |
Time: | 12:41 LT |
Type: | Cessna 172B |
Owner/operator: | Mike Haigood/bill Hardage |
Registration: | N8224X |
MSN: | 17258724 |
Year of manufacture: | 1969 |
Total airframe hrs: | 2220 hours |
Engine model: | CONTINENTAL O-300-D |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Roswell, NM -
United States of America
|
Phase: | Taxi |
Nature: | Training |
Departure airport: | |
Destination airport: | Plainview, TX (KPVW) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:STUDENT PLT OBTAINED WX BRIEFING FROM FORT WORTH FSS AND FILED VFR FLT PLAN FOR X-COUNTRY FLT FROM PLAINVIEW, TEX, TO ROSWELL, NM, VIA HOBBS, NM,. PLT LANDED AT ROSWELL, REFUELED, AND FILED RETURN VFR FLT PLAN. HE DID NOT OBTAIN UPDATED WX BRIEFING. COLD FRONT HAD PASSED THROUGH AREA BRINGING WIND SHIFT AND HIGH GUSTY WINDS. PLT WAS CLEARED FOR TAKEOFF ON RWY 30 AND WAS TOLD WINDS WERE 310 DEG AT 29KTS. AS PLT RELEASED BRAKES ATCT TOLD PLT THAT WINDS WERE 310 DEG AT 39 KTS. WIND GUST RAISED RIGHT WING AND ACFT WAS BLOWN OVER.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | DEN87LA045 |
Status: | Investigation completed |
Duration: | 1 year and 3 months |
Download report: | Final report |
|
Sources:
NTSB DEN87LA045
Location
Revision history:
Date/time | Contributor | Updates |
27-Mar-2024 15:36 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation