ASN Wikibase Occurrence # 373825
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Date: | Saturday 13 December 1986 |
Time: | 08:40 LT |
Type: | Rand Robinson KR-2 |
Owner/operator: | Private |
Registration: | N3762S |
MSN: | 001 |
Total airframe hrs: | 9 hours |
Engine model: | Volkswagen 1830CC |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Mesa, AZ -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PILOT SAID THAT SHORTLY AFTER TAKEOFF THE CONTROL STICK SHUDDERED AND HE FELT 'BACK PRESSURE' ON THE STICK. THE NOSE STARTED PITCHING UP SO HE PUSHED FORWARD ON THE STICK. HE CONTINUED PUSHING THE STICK FORWARD UNTIL IT REACHED THE FORWARD STOPS. DESPITE THIS, THE NOSE CONTINUED PITCHING UP AND THE AIRCRAFT STALLED. THE PILOT WAS ABLE TO ROLL WINGS LEVEL JUST AS THE AIRCRAFT COLLIDED WITH THE RUNWAY. EXAMINATION OF THE UNDAMAGED TAIL SECTION REVEALED THAT THE ELEVATOR TRIM TAB WAS DISCONNECTED.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX87DUJ03 |
Status: | Investigation completed |
Duration: | 1 year 1 month |
Download report: | Final report |
|
Sources:
NTSB LAX87DUJ03
Location
Revision history:
Date/time | Contributor | Updates |
27-Mar-2024 17:45 |
ASN Update Bot |
Added |
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