ASN Wikibase Occurrence # 374016
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Date: | Thursday 23 October 1986 |
Time: | 10:15 LT |
Type: | Piper PA-28RT-201T |
Owner/operator: | Harold Wilkinson |
Registration: | N2853X |
MSN: | 28R7931226 |
Total airframe hrs: | 1470 hours |
Engine model: | CONTINENTAL TSIO-360 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Madera, CA -
United States of America
|
Phase: | Landing |
Nature: | Training |
Departure airport: | Fresno, CA (KFAT) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:DURING A DUAL INSTRUCTIONAL FLIGHT, THE PILOTS WERE PRACTICING A SIMULATED ENGINE OUT PROCEDURE. ENGINE POWER HAD BEEN REDUCED TO 15' OF MANIFOLD PRESSURE. WHEN AN ATTEMPT WAS MADE TO ADD POWER AT AN ALTITUDE OF ABOUT 500 FT, THE ENGINE QUIT. THE INSTRUCTOR TRIED TO RESTART THE ENGINE, BUT WAS UNSUCCESSFUL. THE INSTRUCTOR SAID THAT DURING THE ATTEMPTED RESTART, THE 'HI' PUMP POSITION WAS SELECTED. ACCORDING TO THE FLIGHT MANUAL, 'ACTUATION OF THE HI FUEL PUMP POSITION, WHEN THE ENGINE IS OPERATING NORMALLY, MAY CAUSE ENGINE ROUGHNESS AND/OR POWER LOSS.' NO PREIMPACT PART MALFUNCTION OR FAILURE WAS FOUND.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX87LA025 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB LAX87LA025
Location
Revision history:
Date/time | Contributor | Updates |
27-Mar-2024 19:53 |
ASN Update Bot |
Added |
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