ASN Wikibase Occurrence # 374096
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Sunday 5 October 1986 |
Time: | 01:35 LT |
Type: | McDonnell Douglas DC-10-10 |
Owner/operator: | United Air Lines |
Registration: | N1843U |
MSN: | 46636/309 |
Engine model: | GE CF-6 |
Fatalities: | Fatalities: 0 / Occupants: 0 |
Aircraft damage: | Minor |
Category: | Serious incident |
Location: | Seattle, WA -
United States of America
|
Phase: | Standing |
Nature: | Unknown |
Departure airport: | |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:DURING ATTEMPT TO APPLY GROUND POWER TO ACFT, INTERNAL FEEDER CABLES SHORTED AND MELTED DOWN. INVESTIGATION REVEALED POOR WORKMANSHIP BY CONTRACTED MAINTENANCE PERSONNEL IN MODIFICATION INSTALLATION.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | SEA87IA003 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB SEA87IA003
Location
Revision history:
Date/time | Contributor | Updates |
27-Mar-2024 20:40 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation