ASN Wikibase Occurrence # 374225
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Date: | Saturday 13 September 1986 |
Time: | 09:09 LT |
Type: | Mooney M20E |
Owner/operator: | Private |
Registration: | N1250X |
MSN: | 125 |
Year of manufacture: | 1963 |
Total airframe hrs: | 2667 hours |
Engine model: | LYCOMING IO-360-A1A |
Fatalities: | Fatalities: 0 / Occupants: 4 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Oklahoma City, OK -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Oklahoma City, OK |
Destination airport: | Eufaula, OK (OF7) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PILOT APPARENTLY HAD NEGLECTED TO CHECK HIS ENGINE OIL SUPPLY BEFORE TAKEOFF SINCE THERE WAS NO OIL IN THE CRANKCASE AT THE TIME OF THE ACCIDENT. IF FIVE QUARTS OF OIL (THE AMOUNT THE PILOT REPORTEDLY STATED WAS IN THE ENGINE AT TAKEOFF) HAD LEAKED OUT DURING A FIVE MINUTE FLIGHT, THEN THE BOTTOM OF THE FUSELAGE AND THE EMPENNAGE ASSEMBLY WOULD HAVE BEEN COATED WITH OIL. EXAMINATION OF THE AIRCRAFT AT THE ACCIDENT SITE SHOWED NO SIGNS OF AN OIL LEAK. THE FORCED LANDING WAS MADE ON ROUGH AND UNEVEN TERRAIN. AFTER TOUCHDOWN THE NOSE GEAR CONTACTED A DIRT BANK AND COLLAPSED.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW86LA166 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB FTW86LA166
Location
Revision history:
Date/time | Contributor | Updates |
28-Mar-2024 07:15 |
ASN Update Bot |
Added |
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