ASN Wikibase Occurrence # 375235
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Sunday 20 April 1986 |
Time: | 18:20 LT |
Type: | Day SKYBOLT DB |
Owner/operator: | Private |
Registration: | N23DA |
MSN: | 01 |
Total airframe hrs: | 460 hours |
Engine model: | LYCOMING IO-360-A1A |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Wisconsin Rapid, WI -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PLT THOUGHT HE HAD SUFFICIENT FUEL FOR A 'SHORT TRIP AROUND THE PATTERN.' HOWEVER, SHORTLY AFTER TAKING OFF FROM RWY 29, THE ENG BEGAN TO LOSE POWER. THE PLT ATTEMPTED TO LAND ON RWY 2, BUT ALL POWER WAS LOST & HE WAS UNABLE TO REACH THE RWY. HE LANDED THE ACFT IN A SHALLOW LAKE (IN APRX 5 FT OF WATER) & WADED ASHORE WITH HIS 4 YR OLD PASSENGER. ONLY 1 INCH OF FUEL WAS FOUND IN THE FUEL TANK & ONLY 8 DROPS OF FUEL WERE FOUND IN THE FUEL STRAINER BOWL.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI86FEP04 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB CHI86FEP04
Location
Revision history:
Date/time | Contributor | Updates |
28-Mar-2024 17:44 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation