ASN Wikibase Occurrence # 375300
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Thursday 10 April 1986 |
Time: | 16:20 LT |
Type: | de Havilland DHC-1 Chipmunk |
Owner/operator: | Eugene Jerde And Thomas Mord |
Registration: | N713W |
MSN: | BF-302 |
Year of manufacture: | 1951 |
Total airframe hrs: | 21 hours |
Engine model: | LYCOMING GO480F1A6 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Pembina, ND -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Pembina, ND (KPMB) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PLT STATED THE ENG QUIT BECAUSE THE FUEL CAP HAD NOT BEEN PROPERLY SECURED AND THE FUEL HAD SIPHONED OUT IN FLT.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | DEN86LA113 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB DEN86LA113
Location
Revision history:
Date/time | Contributor | Updates |
28-Mar-2024 18:25 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation