ASN Wikibase Occurrence # 375602
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Date: | Tuesday 11 February 1986 |
Time: | 20:42 LT |
Type: | Cessna 172P |
Owner/operator: | Private |
Registration: | N55386 |
MSN: | 17275172 |
Engine model: | LYCOMING O-320 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Ontario, CA -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Fullerton, CA (KFUL) |
Destination airport: | (KONT) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE OWNER/PLT (PIC) WAS ON A FLT FOR NIGHT & INSTRUMENT CURRENCY REQUIREMENTS. HE WAS FLYING THE ACFT FROM THE LEFT FRONT SEAT WHILE A COMMERCIAL PLT (CP) WAS OCCUPYING THE RGT FRONT SEAT. DRG AN ILS RWY 26L FINAL APCH AT ONTARIO, CA, THE PIC & CP DISCUSSED A CONSTANT 'ON GLIDE SLOPE' INDICATION & ELECTED TO MAKE A LOCALIZER ONLY APCH. THE CP MISTAKENLYSELECTED AN INCORRECT APCH PLATE & ADVISED THE PIC THAT THE MIN DSCNT ALT (MDA) WAS 1060'. THE ACTUAL MDA FOR THE APCH WAS 1240'. WHILE THEY WERE DISCUSSING THE ALT, THE ACFT DSCNDD & STRUCK ELEC TRANSMISSION LINES AT AN ELEV OF 992'. THE ACFT BECAME ENTANGLED IN THE LINES & REMAINED SUSPENDED FOR 4 HRS BEFORE THE PLTS WERE RESCUED.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX86LA117 |
Status: | Investigation completed |
Duration: | 2 years and 2 months |
Download report: | Final report |
|
Sources:
NTSB LAX86LA117
Location
Revision history:
Date/time | Contributor | Updates |
29-Mar-2024 07:26 |
ASN Update Bot |
Added |
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