ASN Wikibase Occurrence # 376080
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 12 October 1985 |
Time: | 17:00 LT |
Type: | Beechcraft A36 |
Owner/operator: | Dr. Rex Hardman |
Registration: | N72060 |
MSN: | E-2184 |
Total airframe hrs: | 300 hours |
Engine model: | CONTINENTAL IO-550-B |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Chesterfield, MO -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Kirksville, MO (KIRK) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PILOT WAS ON AN IFR FLIGHT PLAN FLIGHT WHEN THE ENGINE ALTERNATOR FAILED AND THE AIRCRAFT BATTERY BECAME SO DEPLETED THAT THE NAV AND COM EQUIPMENT FAILED. PILOT WAS ABLE TO DESCEND TO VFR CONDITIONS. HE STATED HE USED THE CHECKLIST TO MANUALLY EXTEND THE LANDING GEAR BUT EACH TIME HE RELEASED THE CRANK, IT TURNED IN A REVERSE DIRECTION BY ITSELF AND HE FANALLY ELECTED TO LAND GEAR-UP ALONGSIDE THE RUNWAY. HE LATER STATED THAT HE DID HAVE THE GEAR HANDLE DOWN BUT FORGOT TO PULL THE LANDING GEAR MOTOR CIRCUIT BREAKER.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MKC86LA006 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB MKC86LA006
Location
Revision history:
Date/time | Contributor | Updates |
29-Mar-2024 12:30 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation