Serious incident Boeing 727-121 N721PC,
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ASN Wikibase Occurrence # 376152
 
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Date:Sunday 29 September 1985
Time:18:40 LT
Type:Silhouette image of generic B721 model; specific model in this crash may look slightly different    
Boeing 727-121
Owner/operator:Ports Of Call Travel Club
Registration: N721PC
MSN: 18997/235
Total airframe hrs:30204 hours
Engine model:P&W JT8D-7B
Fatalities:Fatalities: 0 / Occupants: 71
Aircraft damage: Minor
Category:Serious incident
Location:Denver, CO -   United States of America
Phase: Approach
Nature:Passenger - Scheduled
Departure airport:Puerto Vallarto, OF
Destination airport:(KDEN)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
DURING GEAR EXTN FOR LNDG, THE FLT CREW NOTED A 'LOUD & VERY NOTICEABLE JOLTING OF THE ACFT.' SHORTLY THEREAFTER, THEY ALSO NOTICED THAT A PORTION OF THE RIGHT MAIN GEAR HAD PUNCTURED THE UPPER SURFACE OF THE RGT WING. THE CREW THEN DECLARED AN EMERGENCY & MADE AN UNEVENTFUL LNDG. AN INVESTIGATION REVEALED THE RGT MAIN GEAR ACTUATOR SUPPORT LINK, PN 65-19657-5, HAD BECOME CORRODED & FAILED. THE OUTBOARD END OF THE MAIN GEAR ACTUATOR BEAM THEN PUNCTURED THE UPPER WING PANEL. ALSO A HYDRAULIC LINE WAS SEVERED, WHICH DISABLED THE 'A' HYDRAULIC SYS. MAINTENANCE RECORDS FROM THE PREVIOUS ACFT OWNER ERRONEOUSLY INDICATED THAT IN 1971, THE FAILED PART HAD BEEN REPLACED WITH A NEWER LINK ASSEMBLY, PN 19657-11, WHICH DID NOT REQUIRE AN INSPECTION. CONSEQUENTLY, THE REQUIRED INSPECTIONS SPECIFIED IN AD 68-17-01, REGARDING THE FAILED LINK, HAD NOT BEEN COMPLIED WITH BY THE NEW OWNER. BOEING HAD ISSUED A SVC BULLETIN (727-32-306) WHICH RECOMMENDED THAT LINK ASSEMBLIES WITH PN 19657-5 (AS WELL AS -4, -8 & -13) BE REMOVED FROM SVC & DISCARDED.

Probable Cause:

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: DEN85IA250
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB DEN85IA250

Location

Revision history:

Date/timeContributorUpdates
29-Mar-2024 13:16 ASN Update Bot Added

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