ASN Wikibase Occurrence # 376771
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 13 July 1985 |
Time: | 10:00 LT |
Type: | Boeing A75N1 |
Owner/operator: | Private |
Registration: | N1391M |
MSN: | 75-3407 |
Total airframe hrs: | 2085 hours |
Engine model: | LYCOMING R680 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Earle, AR -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Parkin, AR |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PLT REPORTS THAT THE PROPELLER RAN AWAY WHEN THE ACFT WAS AT 75 FT AGL ON FINAL APCH FOR LANDING AT A PVT AIRSTRIP. THE PLT SAID HE WAS TO LOW TO CORRECT THE PROPELLER MALFUNCTION AND WAS FORCED TO LAND IN A BEAN FIELD ADJACENT TO THE STRIP. AN FAA INSPECTOR EXAMINED THE PROPELLER AFTER THE ACDT AND OBSERVED DAMAGE TO THE LOW PITCH STOPS; HOWEVER THE INSPECTOR COULD NOT DETERMINE WHAT DAMAGE OCCURRED BEFORE THE ACDT AND WHAT DAMAGE OCCURRED DURING THE ACDT.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MKC85LA157 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB MKC85LA157
Location
Revision history:
Date/time | Contributor | Updates |
29-Mar-2024 19:37 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation