Accident Cessna 175 Skylark N7366M,
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ASN Wikibase Occurrence # 37712
 
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Date:Sunday 28 June 1998
Time:01:32 LT
Type:Silhouette image of generic C175 model; specific model in this crash may look slightly different    
Cessna 175 Skylark
Owner/operator:Bill M. Kerlee
Registration: N7366M
MSN: 55666
Year of manufacture:1958
Total airframe hrs:2586 hours
Engine model:Continental GO-300-A
Fatalities:Fatalities: 1 / Occupants: 1
Aircraft damage: Destroyed
Category:Accident
Location:Clovis, NM -   United States of America
Phase: Approach
Nature:Private
Departure airport:Los Lunas, NM (E98)
Destination airport:(KCVN)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The non-instrument rated private pilot (237 hours of flight experience) was a professional truck driver and had worked 12 hours on the day of the accident. The pilot departed at 2200 (he had 5.2 hours of night experience during the last 18 months). The moon set at 2255. Witnesses reported seeing a large spark which lit up the sky on the approach end of runway 4. The power went out at the airport, including the runway lights. N7366M was seen flying low over the runway and applying power to go-around. The airplane was found in a cornfield 1,500 feet left of runway centerline. The approach track to runway 4 crosses transmission lines 3,510 feet from the PAPI indicated runway touchdown point (the three top lines were found separated). It could not be determined if the pilot had training or exposure to the PAPI system. The pilot last flew with his flight instructor (in N7366M) on March 19, 1998; the flight instructor observed that the attitude indicator was not functioning properly. No documentation was found which indicated that the attitude indicator had been fixed.

Probable Cause: The pilot's failure to maintain adequate obstacle clearance and the proper landing glide path. Also causal was his loss of aircraft control during an attempted go-around. Factors were the dark night light conditions, the pilot's recent lack of sleep, and the pilot's lack of recent night flying experience.,

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: FTW98FA287
Status: Investigation completed
Duration: 1 year and 5 months
Download report: Final report

Sources:

NTSB FTW98FA287

Location

Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
21-Dec-2016 19:23 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
07-Apr-2024 09:51 ASN Update Bot Updated [Time, Operator, Other fatalities, Destination airport, Source, Narrative, Category, Accident report]

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