ASN Wikibase Occurrence # 377415
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Date: | Saturday 13 April 1985 |
Time: | 13:30 LT |
Type: | Rotec Rally 3 |
Owner/operator: | Moral Majority Foundation |
Registration: | N316SR |
MSN: | 25475 |
Total airframe hrs: | 47 hours |
Engine model: | ROTAX 503 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Alta Vista, VA -
United States of America
|
Phase: | Initial climb |
Nature: | Unknown |
Departure airport: | |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:EACH TIME THE PILOT APPLIED NOSE UP PITCH CONTROL AFTER TAKE OFF, THE ACFT SETTLED BUT WOULD MAINTAIN STRAIGHT AND LEVEL FLIGHT WHEN THE CONTROLS WERE NEUTRALIZED. DUE TO THE SETTLING EFFECT, OBSTRUCTION CLEARANCE COULD NOT BE ATTAINEDAND THE ACFT SETTLED INTO TREES AT THE END OF THE RUNWAY. THE PILOT WAS EJECTED WHEN THE STITCHING OF HIS LAP BELT FAILED. THE ACFT AS PREVIOUSLY FLOWN SUCCESSFULLY SEVERAL TIMES AFTER ASSEMBLY FROM THE MANUFACTURER'S KIT, BUT ON THE ACCIDENT FLIGHT A 150 LB SAND BAG WAS STRAPPED INTO THE RIGHT SEAT. WITH THE ADDITIONAL WEIGHT, THE SPOILER CABLES TIGHTENED AS THE WINGS PRODUCED LIFT, TO THE POINT THAT THEY INADVERTENTLY DEPLOYED WITH APPLICATION OF AFT STICK.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | BFO85LA039 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB BFO85LA039
Location
Revision history:
Date/time | Contributor | Updates |
30-Mar-2024 11:32 |
ASN Update Bot |
Added |
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