ASN Wikibase Occurrence # 378180
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Date: | Tuesday 30 October 1984 |
Time: | 16:30 LT |
Type: | Hughes 500D/369D |
Owner/operator: | Trafficopters, Inc |
Registration: | N8069G |
MSN: | 02320 |
Total airframe hrs: | 3322 hours |
Engine model: | Allison 250-C20B |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Mc Cordsville, IN -
United States of America
|
Phase: | En route |
Nature: | Unknown |
Departure airport: | Brookside, IN (121) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE HELICOPTER LANDED HARD DURING AN AUTOROTATIVE DESCENT WHILE ON A TEST FLT & CHOPPED OFF THE TAIL BOOM. THE PLT STATED HE LOST POWER AT 150 FT AGL & ENTERED AUTOROTATION. INVESTIGATION REVEALED THAT THE FUEL QUANTITY FLOAT HAD BECOME INTANGLED WITH THE FUEL PUMP ELECTRICAL LINE. THIS RESULTED IN AN INDICATION OF 150 LBS OF FUEL ON THE FUEL GAUGE WHEN IN FACT THERE WAS NO FUEL IN THE TANKS, LINES OR FILTERS. THERE IS A WARNING IN THE MAINTENANCE MANUAL STATING THE FUEL PUMP ELECTRICAL LINE SHOULD BE TIE WRAPPED TO THE FUEL LINE SO AS NOT TO INTERFERE WITH THE FLOAT.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI85FA034 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB CHI85FA034
Location
Revision history:
Date/time | Contributor | Updates |
31-Mar-2024 05:48 |
ASN Update Bot |
Added |
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