ASN Wikibase Occurrence # 378879
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Wednesday 25 July 1984 |
Time: | 14:50 LT |
Type: | Boeing 727-2M7 |
Owner/operator: | Republic Airlines |
Registration: | N721RW |
MSN: | 21200/1206 |
Year of manufacture: | 1976 |
Engine model: | P&W JT8D |
Fatalities: | Fatalities: 0 / Occupants: 127 |
Aircraft damage: | None |
Category: | Serious incident |
Location: | Minneapolis, MN -
United States of America
|
Phase: | En route |
Nature: | Passenger - Scheduled |
Departure airport: | Minneapolis, MN (MSP |
Destination airport: | San Francisco International Airport, CA (SFO/KSFO) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE CREW REPORTED THAT THEY NOTICED A DECREASE IN CLIMB RATE WHILE OVER RAPID CITY, SD, EN ROUTE FROM MSP TO SFO AT FLT LEVEL 310. THE PLT NOTED FUEL BURN WAS APRX 1400 LBS AHEAD OF SCHEDULE. IN-FLT INSPECTION REVEALED THAT THE INBOARD TRAILING EDGE FLAPS HAD FAILED TO RETRACT PROPERLY AFTER TAKEOFF AND REMAINED IN A 7 DEG DOWN POSITION. THE FLT RETURNEDTO MINNEAPOLIS AND LANDED AT 1540 CDT (APRX 50 MINS AFTER THE INCIDENT). A POST FLT INSPECTION DISCLOSED THAT THE INBOARD FLAP CONTROL VALVE HAD FAILED. THE FLT CREW SAID THAT THIS MALFUNCTION HAD OCCURRED ON A PREVIOUS FLT AND HAD BEEN REPORTED. THE FLAPS HAD GROUND CHECKED OK BOTH ON THIS & THE PREVIOUS OCCASION. THIS REPORTED FAILURE WAS CORRECTEDBY REPUBLIC AIRLINES MAINTENANCE BY REPLACEMENT OF A FLAP CONTROL VALVE AND INSPECTION OF THE RIGGING IN ACCORDANCE WITHBOEING MAINTENANCE MANUAL 27-51-51, AFTER THIS INCIDENT.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI84IA314 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB CHI84IA314
History of this aircraft
Other occurrences involving this aircraft
5 February 2021 |
PR-TTO |
Total Linhas Aereas |
0 |
near Florianópolis, SC |
|
non |
16 July 2021 |
PR-TTO |
Total Cargo |
0 |
Curitiba-Afonso Pena International Airport, PR (CWB/SBCT) |
|
min |
Tire failure |
Revision history:
Date/time | Contributor | Updates |
31-Mar-2024 13:21 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation