ASN Wikibase Occurrence # 379093
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Date: | Saturday 30 June 1984 |
Time: | 10:00 LT |
Type: | John R Jones PDQ2VW |
Owner/operator: | John R Jones |
Registration: | N44222 |
MSN: | 113101102B |
Total airframe hrs: | 4 hours |
Engine model: | Volkswagen 1600CC |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Aurora, CO -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE HOMEBUILT ACFT WAS BEING TESTED FOR FLT EVEN THOUGH PREVIOUS TESTS HAD PROVEN THAT THE ENGINE WOULD NOT SUPPORT FLT.THE PLT SAID THE CARBURETOR HAD BEEN IMPROVED PRIOR TO THIS TEST. THE ACFT TOOKOFF AND CLIMBED TO ABOUT 15 FT AGL AND STAYED AT THAT ALT FOR THE LENGTH OF THE RWY. WHEN THE ENGINE LOST POWER THE PLT SAID A LANDING WAS MADE OFF THE DEPARTURE END OF THE RWY. AFTER ABOUT 25 FT OF ROLL THE ACFT NOSED OVER. THE PLT SAID THAT THE LOSS OF POWER WAS DUE TO IMPROPER CARBURETOR NEEDLE VALVE SETTING. THE DENSITY ALT AT THE TIME OF THE ACCIDENT WAS ABOUT 8400 FT. THE ARPT IS 5680 FT MSL. THIS FLT WAS TO HAVE BEEN THE BASIS FOR APPLICATION FOR AN AIRWORTHINESS CERTIFICATE FOR THIS ACFT.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | DEN84FTE02 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB DEN84FTE02
Location
Revision history:
Date/time | Contributor | Updates |
31-Mar-2024 15:42 |
ASN Update Bot |
Added |
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