ASN Wikibase Occurrence # 379264
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Monday 11 June 1984 |
Time: | 14:03 LT |
Type: | Lockheed L-1011-385-3 |
Owner/operator: | Pan American World Airways |
Registration: | N501PA |
MSN: | 193Y-1176 |
Total airframe hrs: | 10064 hours |
Engine model: | Rolls-Royce RB 211 |
Fatalities: | Fatalities: 0 / Occupants: 157 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Los Angeles, CA -
United States of America
|
Phase: | Initial climb |
Nature: | Passenger - Scheduled |
Departure airport: | Los Angeles, CA (KLAX) |
Destination airport: | Miami, FL (KMIA) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:SHORTLY AFTER THE AIRCREW MOVED THE GEAR HANDLE FROM 'UP' TO 'OFF', DURING INITIAL CLIMB, THEY HEARD A LOUD BANG IN THE NOSEWHEEL AREA. THEY RETURNED TO THE ARPT & LANDED AFTER DUMPING FUEL. AN EXAM REVEALED THAT BOTH LOWER ATTACH LUGS ON THE NOSE GEAR CRANK ASSEMBLY HAD FAILED & ALLOWED THE RETRACT ACTUATOR ARM TO PENETRATE THE WHEEL WELL BULKHEAD & CARGO COMPARTMENT FLOOR. A METALLURGICAL EXAM REVEALED THAT THE LEFT LUG HAD FAILED IN OVERLOAD AFTER FAILURE OF THE RIGHT LUG. THE FRACTURE SURFACE OF THE RIGHT LUG WAS TOO BADLY DAMAGED FOR AN EVALUATION; HOWEVER, SOME INTERGRANULAR CORROSION WAS NOTED IN THE REMAINING FRACTURE FACE.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX84LA349 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB LAX84LA349
Location
Revision history:
Date/time | Contributor | Updates |
31-Mar-2024 17:32 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation