ASN Wikibase Occurrence # 380283
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 31 December 1983 |
Time: | 11:00 LT |
Type: | Cessna A150M |
Owner/operator: | Frank Senteiro |
Registration: | N7320A |
MSN: | 150 0713 |
Total airframe hrs: | 1560 hours |
Engine model: | Continental O-200-A |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Castaic, CA -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Private |
Departure airport: | |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:AFTER THE PLT LANDED ON AN ABANDONED ROAD, THE AIRCRAFT WENT OFF THE RIGHT SIDE, NEAR THE END OF THE ROADWAY, THEN WENT OVER AN EMBANKMENT & NOSED OVER. HE DID NOT SUBMIT AN ACCIDENT REPORT (NTSB FORM 6120.1). HOWEVER, HE TOLD SHERIFF'S DEPUTIES THAT HE MADE A FORCED ON THE ROAD AFTER THE ENG LOST POWER. ACCORDING TO HIM, THE ENG STOPPED WHILE HE WAS PERFORMANING A ROLLING MANEUVER, THEN WOULD NOT RESTART. NO MECHANICAL PART MALFUNCTION OR FAILURE WAS FOUND. APRX 9.5 GAL OF FUEL WAS REMAINING IN THE TANKS AFTER THE ACCIDENT. THE PLT INDICATED TO THE DEPUTIES THAT HE DETECTED A TAIL WIND DURING THE LANDING.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX84LA126 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB LAX84LA126
Revision history:
Date/time | Contributor | Updates |
01-Apr-2024 14:54 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation