ASN Wikibase Occurrence # 381248
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Date: | Wednesday 3 August 1983 |
Time: | 13:20 LT |
Type: | Goodyear FG1D |
Owner/operator: | Business Aviation Services |
Registration: | N62290 |
MSN: | 3890 |
Year of manufacture: | 1945 |
Total airframe hrs: | 885 hours |
Engine model: | P&W R-2800-8W |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Crystal, MN -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | |
Destination airport: | Eden Prairie, MN (FCM |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PLT REPORTED THAT DURING THE TAKEOFF ROLL, THERE WAS A SLIGHT LOSS OF MANIFOLD PRESSURE. THIS WAS FOLLOWED BY A LOUD 'MISFIRE', A FUTHER LOSS OF MANIFOLD PRESSURE & A DROP IN THE ENG RPM. WITH AN ESTIMATED 2000 FT OF RWY REMAINING, HE ELECT TO ABORT & USED HEAVY BRAKING ACTION IN AN ATTEMPT TO STOP BEFORE REACHING A ROADWAY. HOWEVER, THE ACFT CONTINUED OFF THE RWY, AND SUBSEQUENTLY, IT NOSED OVER. AN INVISTIGATION REVEALED THAT A SPRING, P&W PN: 153003, IN THE IMPELLER FUEL FEED VALVE ASSEMBLY WAS COMPLETELY DETERIORATED. THE ABSENCE OF SPRING TENSION ON THE AIR SIDE OF THE FUEL DIAPHRAM RESULTED IN A LOW METERED FUEL PRESSURE.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI83FER01 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB CHI83FER01
Location
Revision history:
Date/time | Contributor | Updates |
02-Apr-2024 01:24 |
ASN Update Bot |
Added |
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