ASN Wikibase Occurrence # 381594
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Date: | Monday 27 June 1983 |
Time: | 17:44 LT |
Type: | Enstrom 280C |
Owner/operator: | Private |
Registration: | N652H |
MSN: | 1102 |
Total airframe hrs: | 3362 hours |
Engine model: | Lycoming HIO-360-E1BD |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Kent, WA -
United States of America
|
Phase: | En route |
Nature: | Survey |
Departure airport: | Seattle, WA (KBFI) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:DURING A TRAFFIC REPORTING FLT FOR A RADIO STATION, THE PLT NOTED THE ONSET OF A SEVERE VIBRATION WHICH HE FELT THROUGH THE ANTITORQUE PEDALS. HE STATED THAT WITHIN SECONDS, THE HELICOPTER LOST DIRECTIONAL CONTROL & BEGAN A RAPID, UNCONTROLLED SPIN TO THE RIGHT. REPORTEDLY, THE HELICOPTER TUMBLED OUT OF CONTROL FOR A TIME. HOWEVER, THE PLT WAS ABLE TO REGAIN PARTIAL CONTROL AS IT ROLLED THRU A RELATIVELY UPRIGHT ATTITUDE. BEFORE CRASHING, THE RATE OF DESCENT WAS SLOWED WITH FULL COLLECTIVE & A ROTATING IMPACT OCCURRED IN A HORIZONTAL ATTITUDE. AN INVESTIGATION REVEALED THE TAIL ROTOR DRIVE SHAFT SPLINE COUPLING, PN 28-13609, HAD BECOME WORN. THE TEETH OF THE COUPLING WERE WORN AWAY & THERE WAS IRON OXIDE & CARBONIZED LUBRICANT WITHIN THE COUPLING. THE SPLINED MALE END OF THE COUPLING WOULD ROTATE WITHIN THE SPLINED FEMALE HOUSING. IT HAD ACCUMULATED 149.1 HRS SINCE LUBRICATED. THE LUBRICATION CHART & CHECK SHEET (PAGES MM-3-5 & MM-3-6 OF THE MAINTENANCE MANUAL) SHOW THAT THE COUPLING SHOULD BE LUBED AT 100 HR INTERVALS
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | SEA83FA135 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB SEA83FA135
Location
Revision history:
Date/time | Contributor | Updates |
02-Apr-2024 05:08 |
ASN Update Bot |
Added |
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