ASN Wikibase Occurrence # 382220
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Wednesday 13 April 1983 |
Time: | 11:15 LT |
Type: | Bell 47G-4A |
Owner/operator: | Appalachian Power Company |
Registration: | N4749R |
MSN: | 7650 |
Year of manufacture: | 1968 |
Total airframe hrs: | 4123 hours |
Engine model: | Lycoming VO-540-B1B3 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Charleston, WV -
United States of America
|
Phase: | Approach |
Nature: | Survey |
Departure airport: | Roanoke, VA |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:DURING AN APPROACH TO LAND, THE ENGINE LOST POWER AT APRX 500 FT AGL. THE PLT REPORTED THAT DURING AN AUTOROTATIVE LANDING, HE HAD TO MANEUVER TO AVOID TREES & A RIDGE IN ORDER TO LAND IN A SUITABLE AREA. DURING THIS TIME, ROTOR RPM DROPPED & A CRASH LANDING OCCURRED. A TEARDOWN OF THE ENGINE REVEALED THAT THE TIMING GEAR, PN 67687, HAD FAILED & A TOOTH HAD SEPARATED. ALSO, THE WOODRUFF KEY, PN STD-858, HAD FAILED. A METALURGICAL EXAMINATION REVEALED EVIDENCE OF FATIGUE ON BOTH PARTS. FAILURE OF THE TIMING GEAR ORIGINATED AT AN INNER CORNER OR THE GEAR KEYWAY. THE ENGINE HAD ACCUMULATED 613 HRS OF FLT TIME SINCE MAJOR OVERHAUL.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ATL83LA160 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB ATL83LA160
Location
Revision history:
Date/time | Contributor | Updates |
02-Apr-2024 11:33 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation