ASN Wikibase Occurrence # 382347
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 26 March 1983 |
Time: | 11:11 LT |
Type: | Cessna T-41B (R-172E) |
Owner/operator: | Fort Wainwright Flying Club |
Registration: | N65104 |
MSN: | 67-15063 |
Total airframe hrs: | 5492 hours |
Engine model: | Continental IO-360-D |
Fatalities: | Fatalities: 0 / Occupants: 4 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Healy, AK -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Fort Wainwright, AK |
Destination airport: | Anchorage, AK (MRI) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PLT REPORTED THAT WHILE CRUISING AT 4000 FT MSL, THE ENG POWER BEGAN TO FLUCTUATE, THEN THIS WAS FOLLOWED BY A BANGING NOISE, ROUGH ENG OPERATION & A DECLINE IN POWER OUTPUT. HE HAD TURNED TO LAND INTO THE WIND WHEN THE ENG POWER INCREASED & STABILIZED. THEREFORE HE TURNED DOWNWIND TO ATTEMPT TO REACH A HIGHWAY. HOWEVER, A SHORT TIME LATER, THE ENG STOPPED COMPLETELY & HE WAS COMMITTED TO LAND DOWNWIND & DOWNHILL. DURING THE LANDING, THE ACFT NOSED OVER. AN ENG TEARDOWN REVEALED THAT THE #4 EXHAUST PUSHROD, PN 630393, HAD FAILED. REPORTEDLY, THE WIND WAS GUSTING TO 35 KTS.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ANC83FA059 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB ANC83FA059
Location
Revision history:
Date/time | Contributor | Updates |
02-Apr-2024 13:01 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation