ASN Wikibase Occurrence # 382771
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Date: | Tuesday 4 January 1983 |
Time: | 14:25 LT |
Type: | Douglas A-26C |
Owner/operator: | Garrett Turbine Engine Co. |
Registration: | N25GH |
MSN: | 6934 |
Total airframe hrs: | 2751 hours |
Engine model: | P&W R-2800 CB 16 |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Phoenix, AZ -
United States of America
|
Phase: | Taxi |
Nature: | Unknown |
Departure airport: | |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE LEFT GEAR RETRACTED. THE MODIFICATION OF THE ACFT FOR EXPERIMENTAL USE REDUCED ACCESS TO THE RUDDER TRIM CONTROL WITH THE GEAR SELECTOR IN THE DOWN POSITION. WITH THE SELECTOR IN NEUTRAL, IT WAS POSSIBLE TO APPLY LOADS TO THE GEAR WHICH REMOVED THE GEAR FROM THE POSITIVE DOWN & LOCKED POSITION. POSITIONING THE SELECTOR TO THE DOWN POSITION EXERTS 1500 PSI TOWARD THE DOWN POSITION. SUBSEQUENT TO THE ACCIDENT, THE OPERATOR RELOCATED THE RUDDER TRIM KNOB TO ALLOW RAPID 360 DEG OPERATION OF THE TRIM HANDLE WITH NO INTERFERENCE WHEN THE LANDING GEAR HANDLE IS IN THE DOWN POSITION.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX83FUJ11 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB LAX83FUJ11
Revision history:
Date/time | Contributor | Updates |
02-Apr-2024 17:27 |
ASN Update Bot |
Added |
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